It was a dry day so I decided to take the MG on a 20 minute drive to shakedown any issues. The MG pulled strongly and seemed to run down the road nicely. It definitely prefers to be pulling than pootling and isn’t particularly good at picking up from really low revs. I’ve got free flowing air filters, tubular manifold and a big bore exhaust so I think that’s probably those mods and it just being an older car compared to my (ahem) 400bhp Polestar EV with its instant torque!
On return home the engine was idling nicely so it’s feeling a lot better tuned than before. I did however see a bit of coolant around the top hose and on closer examination it was coming from a joint that didn’t look too good with the rubber host not aligned with the steel pipe. So this evening I loosened the clips and wriggled it into better alignment – not perfect, but better. I’ll give it another run tomorrow and check again.

