3 March 2022 Batch Day #2

Day two of the batch of jobs was again a damp day but we had a gazebo erected over the the MG butted up to the open garage door so were protected from the worst of the elements. Ashley was again on hand to help with the list of jobs.

Gearbox cross-member: We started with what we expected to be a very difficult job which was doing up the bolts which fit the gearbox to the cross-member. This was a job left over from the engine install, over two years ago and was essential for the car to be roadworthy. While recognising that the bolts are very fiddly, Ashley managed to do them both up and it was a bit of an anti0climax really.

Brake bleeding: Next job was to bleed the brakes. A long time ago I had got the system operational (with help!) but I had a soft pedal which needed a pump to get them to go. We bled them using my Gunson pressure kit which worked well and we had a little air out of the system. A later short drive around the block confirmed that we now have a firm pedal and effective brakes, albeit not quite in the same league as my 400 bhp Polestar 2 EV. I will keep a close eye on how its braking and keep an eye out for any leaks. Dad insists I get a low level warning lamp – its on the list Dad.

Fuel tank leak: The fuel tank has been seeping petrol annoyingly for a while when topped up over the level of the sender. I have tightened the sender, and from inspection today it looked like it was seeping from the welded section around the sender, not the sender connection itself. Annoying, as I can’t do anything about a manufacturing fault apart from complain to the supplier (which I will) but even if they give me a new tank, I’ll have to fit it, so not happy. I have bought some tank putty which I may put on as a temporary hold. No solution at the moment, and fuel is rather important to the whole project.

Is that seeping from the seam. It looks like it

Seat fitting: We were feeling really confident about fitting the seats. We had the runners all ready to go, so we offered up the driver’s seat thinking this would be an easy job of simply doing up the backs, then sliding the seat back on its runners and doing up the front. Four bolts – easy! Several hours later and having tried a few different things, including changing up the sequence, and changing a runner, we were still without a satisfactory fit. The basic problem was that we could not get four-bolt to seat runner alignment. We could get two out of four and even got three out of four with a lot of work, but the fourth bolt would not align with the captive threads in the floor. So this is baffling us at the moment and we had to admit defeat of this for the moment pending inspiration. Around the same time we concluded that the old seat belts were really not going to cut it as the mechanism was not operating right and the belts looked well past their best. Safety first, I ordered new from Moss to collect the following morning.

We were nearly out of ideas so decided to stop, think and retry tomorrow

Door cards and capping: While Ashley was experimenting to try to fit the seats I fitted the passenger side door card and capping. The door car is a very simple fit and it went on like a treat. These are second hand ones that I fitted and I am pleased with them. The door capping, which is a chunky piece which fixes to the door top screwed on nicely. I was feeling chuffed until I noticed a gap around the door handle and realised that the I did not have the escutcheons – darn! Another thing to add to the Moss order

It’s starting to look like a car!

Road test: A start up (best avoided usaully) had been essential today as we had the car up on ramps. So as our working day drew to a close, its seemed justifiable to run the MG around the block. Gingerly backing off the ramps I reversed onto the road (I am fully insured) and waited while Ashley jumped in (sitting on the floor). I was in the drivers seat which had three out of four bolts, was fully back (a bit too far) and with no belts. We weren’t planning on going over 15 miles per hour so I judged this to be okay. First to test were the brakes which pulled the MG up nicely. Otherwise, the test went fine, the MG pulled cleanly, although the steering feels really heavy and the large wheel is in the way of my thigh. I have a wooden wheel just needing the correct boss, so that will improve things.

So a few more jobs to do tomorrow to conclude this three day burst. Ashely has been brilliant, a calm, considered, clever and strong par of hands to lend to the long list of jobs. We’ve made good progress.

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