21 Nov 20 Wiper Motor and other bits and bobs

In early December I have a classic car auto electrician coming to look at the loom on the MGB and to help with its installation. He’ll carry out an assessment first, and then recommend what he is able to do. In readiness for this, I rolled the MG out onto the drive on this sunny November afternoon. Before I got on with the neccessary work, I couldn’t resist firing up the MG. She started on the second go, so the battery had held out, which is encouraging in terms of the alternator actually working. I had a bit of a fiddle with the idle speed and mixture and managed to get it idling relatively smoothly with the choke fully in engine warmed up. I am not kidding myself that the carbs are set up, but at least its running better than when initially started a few weeks ago. I am a bit addicted to the noise and couldn’t resist a couple of revs. My neighbour’s grown up son came to see what the noise was and he liked what he heard!

The preparation on the loom today consisted of me undoing the jerry-rigged set up I had created to get the car started. The loom was basically resting in the foot well which is clearly not right. I disconnected the ignition switch (having taken numerous photos) and various other connections including several temporary earths. I then took a good look at the loom and carefully unravelled it to lay behind the dashboard in roughly the right configuration. I then looked at where the loom enters the interior and identified the correct location of the first earth connection. Having learned that stainless steel does not have as good connectivity as mild steel, I didn’t use a fresh shiny bolt but dug out an old one from the bolt box. That led me to contemplate the wiper motor which is just under the dash on the off side (UK). The wiper motor was dangling awkwardly from the drive cable so needed to be fitted properly in its mount. First I tightened up the drive cable connection to the motor as this was only half on. I then offered the motor up to its mount, noting that the angles didn’t really work, but it was possible to persuade it in. The motor is mounted by a steel hoop, but to keep it in snug there are two rubber elements – a pad which goes against the bulkhead and a lining to the hoop. Getting these to align and stay in place as I tightened up the two bolts was tricky to say the least, but I managed it after a couple of attempts. So with the wiper motor in place I was able to fit the earth connection I had spotted earlier. Due to the exact positioning of this, effectively under the scuttle, and the bar runs below the dash, this wasn’t that easy – I had to sit on the floor with my back to the car and feed my hand through the various obstacles and then get the right angle. Hopefully, that can stay there now for the duration!

I also greased the speedo cable in anticipation of connecting this up in the near future. All the while I was listening to a radio adaption of Ian Flemming’s James Bond in Moonraker. A great afternoon.

15 Nov 20 Replacing the alternator

A surprisingly sunny November morning appeared from what I had thought was a write-off rainy weekend, so it was out with the MG to swop out the old alternator with a new one from MGB Hive. When I first got the MG, the alternator was covered in white aluminium corrosion crystals. I scraped off the worst and when I fired the car up (this was 3 years ago) for the first time, there was a flurry of white as the loose crud spun out. Suffice to say I thought the alternator had seen better days and so having recently restarted the engine I decided to replace it. Also prompting me to this job was that whenever I have run the car recently, it has flattened the battery. This was either because the old alternator was not working properly, or because something wasn’t wired properly. As I was going to replace the alternator anyway, I tried this first.

The alternator is held in place with two bolts at the top, which mount onto lugs on the engine block and with a single bolt at the bottom which secures a curved slotted plate. The slotted plate allows the alternator to pivot so that the fan belt can be fitted over the pulleys and then tensioned correctly. The slotted plate then fixes to a lower lug fixed to the engine block. The lower lug is fixed with a specifically shaped bolt which I had replaced much earlier in the rebuilt when it had sheared off spitefully on removal. Before I took the old alternator off, I started the engine and measured the voltage at the battery – 12.3v.

Fitting the new alternator was pretty simple although it’s a heavy old bit of kit. I did a visual comparison before I removed the old one just in case it was to join my list of wrongly ordered parts, but it measured up alright so I committed to the job. I laid a decent blanket over the wing for protection and knelt on a tool box with a blanket on it for comfort. I used a combination of tools to remove the bolts which were 0/5″ and 9/16. This included my trusty Halfords Professional mini socket set, the Elora large socket set gifted to me by my friend John, the socket spanner set gifted to me by my brother Tris and a plain open jawed spanner. Each tool works well in its own way and I was grateful for the choice.

With the new alternator fitted and the fan belt at roughly the right tension, I fired up the car again. It fired second time and settled into a lumpy idle (carbs still not set up right – where are you Dad? ha ha). I tested the voltage at the battery and got…the same 12.3v. I was hoping for between 13-14v but I could be wrong. So maybe the issue is not solved. I should have had someone hold the revs higher and measured it again, but Helen was working in her study, so I didn’t disturb her. So we will see if the battery is flat when I try again. Hopefully next weekend we will get another weather window for further investigation. Before sitting down to do this update, I sent a web enquiry to a mobile auto electrician just to gauge their interest in giving the electrics a once over and validating what I’ve done. I think it might be worth getting a professional involved in this one…

7&8 Nov 20 Starting progress

One advantage, perhaps the only advantage of lockdown is that we are forced to stay at home and not go ‘gadding about’ as we are normally inclined to do. So it was that after a most pleasant stoll in nearby Cirencester Park, Gloucestershire, as part of our permitted exercise, I found myself with a sunny late autumn afternoon to dedicate to the MG.

I decided to sort out the choke spindle on the carburetters (carbs for short) which I had managed to fit the wrong way around. What I haven’t recorded here is that I had previously corrected the throttle spindle which I had also fitted the wrong way around. Such is the lot of first time amateur car restorers such as myself, progress is riddled with little mistakes, however, with each mistake, I try to learn something. So to the choke spindle, which is an assembly comprising a spindle which sits within a cup on each carb (the MG has two). The choke mechanism operates when the choke handle is pulled on the dash. This causes the cable to tighten which, being attached to a lug on the spindle causes it to rotate. This rotation causes the choke mechanisms on both carbs to be operated because the ends of the spindles have lugs which fit onto the cams which themselves are on the end of the choke mechanism. The choke mechanism moves the needle inside each carb to richen the mixture, but also opens the throttle because the cams connect with a screw on the throttle spindle.

The fun begins when you realise that the spindles are not held in place in any way other than sitting in the cups on the carbs so when fitting the carbs you have to align the spindle ends (4 in total, 2 for the throttles, 2 for the chokes) with the cups, and have them aligned to the lugs (again 4 in total) while you are trying to to wriggle the carbs onto the mounting studs (4 in total). I make that around 12 points of contact which you are having to manage and it was certainly easier when I was able to phone a friend. To reverse the wrongly installed spindles, I loosened the carbs, but wanted to avoid taking them off as then you have to do the full accordian player impression as the two carbs writhe in your hands. The carb mounting studs are worth a mention, being located cruelly in the most awkward position and in perilous proximity to the razor sharp edges of the heat shield. It would be good to have three elbows on your arm at this point rather than the inadequate one we have to deal with. I won’t bore you with a blow by blow account, but suffice to say I got it all done in two attempts and only one skinned knuckle. I then fitted the air filters and went for a start up.

I connected the battery (ignition switch solution still pending), heard the familiar ticking of the fuel pump and turned the key. One click and then nothing. Mmm. I tried my spare battery, and it cranked over willingly but wouldn’t fire. Then I remembered to reconnect the coil wire I had disconnected. This time the engine started straight away, with full choke of course, and settled at a fast idle. After it had run for a minute or two I pushed the choke in and tweaked the idle speed to get it to idle correctly. I recorded the sound of the engine in the YouTube clip below. To get the authentic bass – use headphones. For an MGB is does sound rather tasty. Its obviously not set up right just yet, but it’ll do for the moment.

So that was a reasonable afternoon’s accomplishment. Today (Sunday) was a more gloomy day both weather and progress wise. A dull autumn day dawned and after finishing off the chores and watching Church online (another COVID consequence) I pushed the MG onto the drive intending to fit the engine fan I had bought recently. To get access to the pulley I determined it would be neccesssary to loosen the radiator and pull it away from the area. This is relatively simple on the MGB, being six 0.5″ bolts (what else) to remove. Having pulled the radiator back I realised that the fan I had bought was the wrong one – annoying as I thought I had searched it correctly. More catalogue searching required and another item for my MGB parts shop which I will be opening at some stage to sell on all the surplus parts I have amassed over three years. So I had to pointlessly put the radiator back again. It was then I remember that fitting the radiator is more difficult than removing it. The radiator is mounted by the aforementioned six bolts to a steel shroud which is fixed with eight bolts to the inner wings. The challenge is to get this all to align. The shroud in my MGB, despite being resplendant in shiny black from the paint shop, is I believe a bit warped. The off side is particularly difficult and I had to loosen all the bolts on the radiator and shroud on that side to get each bolt to bite on its thread. Having had this difficulty before, I was up to the challenge this time, and a bit of thinking and remembering got the job done in the end. All helped along by my Radio 4 soundtrack in the background, latterly a re run of ‘Just a minute’ with the late Nicholas Parsons.

Thanks for reading – God Bless and Stay Safe.

4 Oct 20 Milestone #2 Engine Start – Achieved

So the title of today’s entry gives away the punchline, but suffice to say I am very pleased to have managed to start the engine today. Woohoo! As a quick recap, I had to send the carbs away as they had been incorrectly re-assembled when they were refurbished. I’ve had an explanation from the company boss that they were installed as they came in. Err, that will be me then. However, all I had done was to take the carbs apart, decide they were in a shocking state and send them away to be rebuilt. Anyway, its all good now and that’s the main thing.

As always with this project, there were some hurdles and hiccups along the way, mostly my fault as we will see. Firstly I removed the carbs from their wrapping. They had been thoroughly wrapped but of course as they were not on the heat shield, but separated so I had to do that thing where you put the linkages together and then hold it all together as a loose assembly as you carry it over to the car and mount it on the studs. In my enthusiasm to get it started, I fitted the throttle linkage upside down, only discovering this after I had awkwardly installed all four nuts and tightened them up. The nuts are extremely awkward to fit – to get the nuts onto the studs the carbs need to be slid up to near the tio to clear the carb body. The two under the carb are even more awkward. Still at least I have now had plenty of practice. Still impatient to attempt a start, I interupped Helen from her work educating the youth of today (yes, secondary school teachers work on the weekend) and asked her to crank the engine over while I manipulated the choke and throttles. On the second turn of the key, the engine fired, but didn’t catch. This was a promising sign, so Helen cranked again and this time I caught it on the throttle and we had a spluttering rev, and a bit of popping. A third attempt resulted in steady fast running with choke and throttle applied. A little exhaust smoke was rising into the engine bay and it was a it of a smoky affair all round. Having relieved Helen of her responsibility as chief cranker I set to to correct the linkage mis-assembly.

I was determined that to turn the linkage around to its correct orientation I wasn’t going to remove both carbs. Instead I removed the front carb, and loosened the nuts on the rear carb. This gave me enough fiddle room, just, to swap the linkage around and then to enjoy the fun game of ‘put the the nut on the stud under the carb bonnet’. It really is a dexterity test and took a bit of trying, but I got there in the end without breaking down in tears. With the linkage in the right way, I could connect up the throttle and choke cables and start the engine in the usual way from inside the car. When I say, the usual way, the ignition switch is on the floor of the car, so not exactly usual, but I didn’t say it was perfect. The car started on the second attempt and I was able to walk around to the front while it ran and see if there was anything amiss. The engine was running fine with full choke but started to splutter as soon as I reduced the amount of choke, so not sure if it was still a bit cold, needs setting up or a bit of both. Anyway, this was a test and I didn’t want to push my luck, so with a quick look around the engine bay I knocked the choke off and let it stall.

So issues identified to investigate today included:-

  1. Loose alternator bolt – tightened
  2. Noted broken cores in the Earth cable to the battery – need to order a new one
  3. Coolant level dropped – top up and check

So we have achieved ‘Engine Start Milestone’ which I set quite a long time ago. Next Milestone I am setting myself is ‘Dashboard Complete.’ This is a complicated one which is going to involve fitting all the gauges, the windscreen wiper system and the Heating and Ventilation System. However, it’s the next logical step and certaintly needs doing before any other interior work is undertaken. Thanks to all of you have journeyed with me towards this milestone. Your support and practical help have been invaluable. God Bless.

12 Aug 20 Releasing the carbs

Having established at the weekend, with Matt’s help, that the carburettors were blocked, and having consulted the ‘MG helpline’, A.K.A. my Dad, I found time this evening, with the help of my friend John, to investigate the problem. The UK was in the middle of a heat wave, one in which the temperature and humidity peaked between 5pm and 6pm arond 30 degrees, which was when we started to look at the MG. So the only right thing to do, while we wheeled the MG out, was to crack open a couple of cold beers and take a leasurely look at the problem. With John on board, this was going to be a logical approach to problem solving. Having already proven fuel would flow up to the carbs, we now knew the challenge was with the carb itself.

Step 1: Use a footpump to attempt to blow air into the carb. Result: No air passing through. Conclusion: Float/Needle valve stuck

Step 2: Remove carbs. Removing the carbs in theory is easy, its just four nuts. In practice, its fiddly, because the nuts won’t come off without waggling them to the end of the studs and then getting the angle just right. Having two people on hand is a definate advantage here, unless you are an octopus. Next challenge was to keep the carbs together with the linkages intact. To do this, we had the idea to use the plate that holds the air filters as a sort of jig. That took a bit of work to get right, but without (much) swearing, the carbs rattled free of their studs and were on the work bench.

Step 3: Remove float chamber lids. These come off easily enough, although the ‘O’ ring on the front carb hopped out of its slot and showed little enthusiasm to pop back in. Using the footpump and with the float valve open we used the foot pump again to add pressure and with a nice ‘pop!’ the needle valve on the rear carb freed itself. Surely the front carb would do the same, but it wasn’t shifting, so John tickled it with a pair of fine tweezers and before long both carbs were wheezing along in harmony at each press of the pump. How satisfying.

Step 4: Reassemble and refit the carbs. Hmm. That float chamber ‘O’ ring did not want to play ball and needs to be replaced, however, we think we teased it back in place and made a seal on both float chamber lids. We then man handled and wiggled the carbs back onto their studs, tightened them up and connected the breather pipe, fuel line, throttle and choke linkages.

Step 5: Test start the engine. ‘Hang on a minute,’ said John ‘didn’t you say that the fuel pump and coil are always on when you connect the battery?’ A discussion ensued in which John advised me against firing the engine when we are not confident of how the wiring was configured. So we disconnected the ignition switch and using a multimeter, identified what the various terminals were and then attempted to connect the correct wires. As we were nearing a conclusion on this, the rain came in heavy so we abandoned the task for the day having made some actual progress, but with some work to go to achieve sustained running.

9 Aug 20 Fuelling around

So having demonstrated that the MG would start, it was time to connect up the fuel pipe and provide a reliable supply to the carbs to sustain running. I had a reliable assistant in the form of Matt (Ellie’s boyfriend). First we bought some fresh fuel and charged the tank with 5 litres. Next we connected the fuel pump wiring, connected the battery and heard a reassuring tick from the pump (err, surely after you turned on the ignition…). After a short while we were concerned that no fuel was flowing through and sure enough, on checking I found the pump was plumbed the wrong way around. I wonder who did that?

After a bit of replumbing and we were back in business although still there was no fuel feeding through to the filter let alone the carbs. Vaguely remembering something about air locks we released the pipe at the carbs end and with a hiss we started to see fuel travelling through the filter and turn up to the carbs. Progress!

But this wouldn’t be the Relentless Duck blog without some ‘issues’ and without detailing all the challenges, we did have a leak out of the fuel sender unit. Not being sure why this was leaking we set up a fuel can to catch the drips until the level was low enough for it to stop. The following day, on a break from work, a YouTube video showed how this should have been tightened up. Another day, another thing learned.

With fuel to the carbs, surely the MG would now fire up and continue running? Sadly not, the carbs refused to take the fuel and the removal of the lid from the float chamber revealed it to be dry. Oh dear. Further investigation needed, the outcome of which will be covered in a future post

07 Aug 20 ENGINE START!

I don’t really approve of ‘shouty’ capitals, but I think this entry justifies their use, albeit in the title only. Today, on my 50th birthday, we achieved the Engine Start Milestone. Let me qualify that a bit. When I say ‘we’ I mean, my Dad, mainly. When I say the engine started, I mean just that – we got it to start, but not run. This was principally because to fuel it, we were not using the main tank, but a borrowed fuel bottle hung from the bonnet catch. But it did fire up, several times and briefly make a loud ‘vroom!’ before ceasing when the fuel we had poured down the throat of the carburettor was consumed. The important point is – it starts!

So today being my 50th birthday, we had invited some close family over within the COVID regulations – so a much smaller group than usual and with the requisite social distancing. My darling wife Helen had, as usual, put on a lovely spread and guests arrived and were dining al fresco in the relaxed garden setting under the Gazebo. After waiting for what seemed to be a polite period of time, Dad said to me ‘what about the MG then’ and we discretely retired to the garage to scratch our respective heads on the non-starting issue.

Dad focussed on getting the electrical side of things sorted and this involved correctly wiring the distributor and setting the timing. This took longer than it should have done, which isn’t very interesting to record here, however after muc removal and refitting of the distributor cap and HT leads we had a spark occuring at the right time but no starting of the engine. We turned out attention to the fuel bottle and suspicious that fuel was not actually getting into the carbs, we poured (I should say, carefully measured a precise quantity of fuel) fuel into the throat of the carbs and turned the engine over. With a vroom and a puff of smoke out the exhaust the engine fired for the first time in over two years. Yes! So I am grateful to Dad (and Matt my Daughter’s boyfriend) for this birthday treat! It was all very exciting. We fired it a couple more times to see see if we could maintain the running before concluding that actually some fresh fuel in the tank and connecting the fuel pump was probably the way to go. Sadly we had run out of time, so this job was deferred for next time.

So this is a great encouragement – I’ve had a lovely birthday, which really started on Wednesday with a visit from my oldest (he not old, but I have been friends with him for the longest time) friend Phil, then a surprise gift and cake from my work colleagues on Thursday, leading to today’s event. Tomorrow we have friends over to continue the celebrations, again reined in by the regulations to a very small group. I heard someone say that birthdays should be a three day event – I’m on four days and going strong!

1 Aug 20 a step forwards

I’ve had a problem with oil leaking from the oil filters area for a while and this has prevented me progressing the engine start because cranking the engine resulted in a pool of engine oil under the car. Having had several goes at refitting the oil filter to oil cooler union, today I used my brain and had Helen in the car cranking the engine over and me looking to see where the leak was coming from. Turns out the leak was from the oil filter ONTO the connection so I was looking in the wrong place. So my focus turned to sorting this connection out and following a phone call to Dad I removed and refitted it. No leak on cranking! Problem solved. I couldn’t resist cranking the engine over to fire (which it didn’t) but I did check and I was getting no spark so at least I know one of the problems to sort out.

This lovely engine bay will sound nice too one day
Oil everywhere but where from!

Back to earlier in the day and ongoing (and off going) saga of the doors and their glass. I had previously fitted the quarter lights but on inspection the runners were perished so I recently ordered some new one from Moss and had stripped them down. So while British Grand Prix Practice and Qualifying ran on I sat in the lounge working the new rubbers into place using a blunt ended tea spoon. Apart from where it dug into my palm painfully it wasn’t too bad and I followed the general approach that Andy from Wiltshire Windscreens showed me when he fitted the front and rear screens. So with these done I loosely fitted the back in. I will tighten them when I get the glass as I think you need them loose to get the whole mechanism in and then you tighten it all up.

Also in preparation for the glass (which I need to order) I removed the lower bracket from the rear glass stay. I have ordered new ones of these with nice new felt lining but they don’t come with the bracket. Rather than put the old brackets on as they were. I decided they would be better painted. I used a Hammerite black straight to rust paint, brush applied. It doesn’t need to look good but it should be protected against corrosion hence this approach. I was a bit delayed in fitting the stays as the paint is still drying so I will need to fit those when I next get the MG out.

Waiting for these to dry before fitting

So that’s about it. Keith the TV aerial guy was passing with his mate and said Hi. A couple of other people nodded their appreciation (or sympathy or contempt it’s hard to tell) so it was an encouraging day on the MG. Last thing to say is that to save my back I towed it out the garage this morning with my CRV which worked reasonably well although I did need a willing assistant which was of course the ever patient Helen.

A closing thought about gratitude…

30 Jul 20 Putting my back into it

I was motivated to get outside after work today and do something useful on the MG. I have for a long time bemoaned how I routed the rear loom which turned out to foul the internal trim panels due to a temporary cognitive failure on my part. So I decided to reverse this and find a better route. Reversing the install turned out to be much simpler than I thought.

I then had to work out a better route and curiously it is remarkably unclear what this should be. After a bit of trial and error I have found a route which allows the loom to reach all the right places and also looks like a reasonable location to be clipped in place out of the way and logically. At least I hope so.

It was good to make some progress after having had a lot of (admittedly not entirely unpleasant) distractions. The only down side was a twinge in my back as the MG is getting heavier the more parts I bolt on, and my back is getting no stronger. I may revert to towing it up the drive until she’s a runner.

5 July 2020 Lockdown delays

I remind myself that this blog is primarily intended (solely intended?) to record the restoration of my MGB GT. As such I should stop worrying about lack of progress, and instead record what I have been doing lately and focus on that. This is what I have been up to.

Despite some clear instructions from the old man regarding setting the timing with the second hand distributor, I havent yet got any life out of the engine. To be honest, on my last attempt I wasnt sure I had the timing quite right and it was a bit of a half-hearted attempt. Also, the oil leaked from the oil cooler to oil filter union again despite me adding the washer so something is not right there. The old man things there should be two washers at this union but that’s not what the book says, so not sure. All I do know is that when turn the engine over, it leaks at this union so something is not right. With lockdown beginning to ease, I might get my mate Mark to take a look as he lives just down the road.

On a recent half day on the MG I got fiddling with the doors and the vexed issue of the door glass. I have been struggling to get this to align and to get the regulator to operate correctly. I can get the window in the door and to go up and down but not fully down or up. On my last go at this, I loosened the rear window channel and found that as this had simply been sprayed over in the pain shop, that when removed, there was rusty metal underneath. I removed the rear channels on both doors and used hammerite ‘straight to rust’ paint to seal over the messy metal. I then ordered two new channels from ebay, which have subsequently arrived and need to be fitted. They have new linings, are not rusty and I hope will assist with fixing the glass.

I also removed the quarterlights as I wasn’t happy with how these were fitted. I obtained a quote of around £400 to refurbish them both, which I thought was a bit steep, so I will order new rubbers seals and fit these myself. This will leave one rubber seal in not great condition (on the actual glass), but that will have to be an item for the running repairs/restoration list. I stripped the quarter light and removed the main rubber seals which were very cracked and in poor condition. A clean up and new rubbers will see these go back in better condition. Its also been interesting to strip these to understand how these go together.

I made an enquiry to a local trimming firm who couldn’t help with the roof lining, but recommended two other people, one who had already failed to respond to an enquiry and one who I have yet to contact. Something to progress as I want the roof lining done by a professional.

I also recently purchased new seat rails as the ones I had were incomplete. I am holding off fitting the carpets and hence the seats until I have got the headlining done and sorted more of the electrics so that it is all tucked away.

So I have not been idle, but just not that productive on the MG during this lockdown period. To my future self I say this: the 2020 lockdown was a weird period. Following initial concerns about my employment, work settled into a work from home routine, and actually in the last two months my team and I have exceeded previous business outputs to achieve some remarkable achievements, not without some personal impact in terms of stress and workload. We have however, maintained security of employment, something I am very grateful about. Furthermore, I have prioritised time with Helen and we made good use of the fine weather while it lasted. I have taken on the role of chair of our Church PCC and DCC, joined a house group which meets weekly for Bible study via Zoom, participated in Helen’s work quiz each Wednesday and caught up with people either in person via social distancing or online. We have cleared our loft, filling an 8 yard skip and selling around twenty items on Facebook and Ebay, raising about £300. We have moved our eldest daughter into a new flat in London. We have socially distance-visited our family. I have managed the Trigg fleet of cars with multiple trips to garages for the Cappuccino, loaning of my CRV to Helen’s sister Kate and cleaned and polished Helen’s Jazz. The first few weeks of lockdown were all about uncertaintly and the novelty. The latter period has been more of a test of resilience, and now we are working through the loosening restrictions and working out what that means.

So when I wonder why progress on the MGB has slowed, I will remind myself that I’ve been a bit busy.

28 Apr 20 Daft cat

Just a quick entry to record this picture of our daft cat. My daughter popped into the garage to access the freezer and as often happens, the cat dived in to poke around the garage in search of a mouse (although she is a useless hunter and there are no mice in the garage, unless you count the 2 x frozen mice we have kept for the in-laws pet snake for when lockdown is over). Anyway, standard procedure is to close the door and leave her in there for ten minutes. She’s usually ready to come out. But tonight she decided to stay in the MG and Lou managed to capture this shot – daft cat. Pity she can’t sort out the timing!

Stay safe folks – God Bless

12 April 2020 What a nut

A couple of hours on the MG this beautiful sunny and warm Easter Sunday and I was focussed entirely on one task and one task only. This was to get a nut onto the threaded trim connector which was poking through the front o/s wing right on a seam which prevented me getting the nut onto the thread. I jacked up the front, placed an axle stand under the car and removed the front wheel to get better access to the thread. I then spent about an hour using including a hammer and dremmel cutting wheel to slowly but surely make space for the nut to fit on. It sounds easy now as I write it, but it was blooming difficult. Ideally, I would have turned the whole car upside down and sideways as this would have made the whole job easier, or at least ‘put it on a ramp’ as my Dad sometimes says (that fully equipped workshop being someway down our family list of priorities). One of the issues was that surprisingly the deep recesses of the front wing are a little dark and so I had to improvise a lighting solution. See pictures below for reference. I finally got the nut to bite on the thread (Halleluiah!) and from then on it was simply a case of tightening up the nut until the trim sat snuggly on the front wing. I had read in my restoration book that it was possible to snap these threads so I was very cautious in tightening it up and decided against jumping up and down on an extension bar which I am not sure is ever a good idea. A satisfying time overcoming a problem while I listened on Radio 4 to a profile of the new Labour leader Keir Starmer and some other analysis of the Coronavirus pandemic.