12 March 2022 Fuel’s errand

I’ve had a fuel leak / seep from the petrol tank for a long old time and today I got it sorted. I suspected the seam where the sender unit goes in, but to be honest, I wasn’t sure I had the sender in properly or the filler spout. I had obtained a replacement tank from the supplier which was a larger ‘touring’ unit so a swap was on the cards in any case. I was on my own today so not the easiest operation. I began with jacking up the rear and putting it on axle stands which enabled me to remove the end section of the exhaust which bolts on about midway along the car and is then attached to a rubber hanger at the other end. Then I detached the fuel line and with the tank propped up on a couple of boxes I undid the bolts and nuts on a diagonal pattern which sort of allowed it drop in a controlled manner.

Now to fit the new tank, but learning from previous experience I took great care to fit the sender, the rubber seal and sealing ring to the tank, and to slop some petrol in and check for leaks before it went anywhere near the car. Miraculously the new tank could hold petrol and I had confidence the sender was properly seated in place. Now for the awkward job of offering up the tank to the receiving bolts (fixed to the chassis) and simultaneously dropping the bolts from the boot floor through the brackets and lining up the threaded connectors. I needed to have a couple of extra hands, but with none being available I did my best octopus impression and managed to have all the nuts, bolts, washers and connections properly done up. The fuel line was easily fitted, so it was onto the exhaust. This was another job which was fiddly to undertake solo. It took me a while to get this done – the bolt up connection at the midpoint is easy enough, but the rubber hanger where the exhaust exits is seriously fiddly. The bolts just did not want to bite and the rubber hanger was pulling the bracket away from where they needed to be. Furthermore, the sun was streaming in my eyes making it difficult to see the holes. I had to drape a throw over the back of the car and crawl underneath just to see! Helen came home from popping out to see my feet sticking out from under the car with a cloth draped over it. She must have wondered what on earth I was doing. I refused to be beaten and just persevered until eventually I got one bolt and then the other started. Then it was just a case of tightening everything up which was tedious as the threads were long and the bolts were tucked up between the fuel tank and the exhaust (I did say a little prayer – so, thanks God). There followed some very tedious petrol movements while I harvested the petrol I had only recently put in the old new tank, but finally I had a working fuel system.

Looking up at the tank fittings

A long time ago I realised that I was missing some chrome trims from the B-post of the MGB and last week they literally fell out of a box at me which saved me from fretting about where to get new ones from. I was looking for a different profile of trim, but these turned out to be the right ones. I fitted these relatively easily earlier today, giving them a brief polish before fitting them with self-tapping screws. I had intended to rivet them on, however the space was a bit tight, so screws it is. This has finished off another aspect of the MGB nicely.

Last job of the day was to fit the wooden wheel which my friend John had lent me ‘on approval’. I had established that this would fit (with a new boss) and the smaller diameter would give me more space for my legs which are wedged up against the steering wheel in the standard configuration. I popped it on the splines and tightened up the nut. I still have to install the horn switch, but that was enough for today.

I finished off the day with a quick test drive of about 2 miles (brave!) with Mrs T on board. This was Helen’s first time in the car and the first time I had driven it out of our estate in the three years I have had it. It was also the first time the car has driven more than about quarter of a miles in around ten years. I had already warmed up the engine and done some checks looking for leaks and we were good to go. Its quite intimidating driving a car that you’ve restored for the first time, being conscious of everything that can go wrong I suppose and also nervous of other traffic. However all was well and were were able to go through the gears into fourth and to cruise very briefly up to 50mph. The drive illustrated a few things, firstly that the hatch needs to be finished off with the rubber seal I have bought and the catch adjusted to stop it banging up and down, and the carburettors need tuning as the car is not pulling cleanly through the revs. The gearbox was a pleasant surprise, being nice and slick to shift although I dig get a ‘box full of neutrals’ at one roundabout while I grounds the gears. Fortunately, the MGB is torquey enough to pull out of the roundabout in third, although this coincided with the flat spot I mentioned so we sat at 32 mph with a BMW following curiously behind on our 50mph limit bypass. Helen commented favourably on the comfort of the seat, but noted the loud exhaust. With the car only partly trimmed and with a lot of grommets still to locate, I think I can tone down the noise a bit, and also I need to check the exhaust it properly done up. have to say, it does sound good and was turning heads. A good day!

5 April 2020 Door glass

A fine spring day (Sunday) as the COVID-19 lockdown continues. With the engine start programme on pause, I decided to continue refitting some of the extensive exterior trim on the MG. Having recently taught myself to pop-rivet, and finding out that is the most fun thing ever, I continued to fit the chrome drip rails and today managed to complete both sides. Just one clip missing which will either turn up or I’ll have to buy from Moss. I then turned to the door glass which I have been wanting to fit for a while. Unfortunately, the door glass is very badly scratched (I don’t know how) so I will need to replace them, however, I decided that there was merit in having a go at fitting them anyway as a sort of trial run for when I get the new / second hand ones. Tricky to justify buying new glass at the moment as I can’t collect from Moss (shop closed) and the cost of shipping glass is blooming expensive. Also, I would have to pry off the metal rails which looks tricky, so maybe I’ll source some second hand units via Ebay for as long as that remains. Anyway, back to today’s efforts which went alright actually. I had to remove the quarter lights and then reaquaint myself with the lifting mechanism which is a bit fiddly. I just looked at it and fiddled it around a bit until it fitted – it took a couple of attempts, I then dropped the windows in and they seemed to slide up and down quite convincingly After checking on YouTube I find that I haven’t hitched the glass properly, so something to sort out tomorrow on my day off.

Lots of people say hello as I’m working out the front on the drive, but one visitor today didn’t really understand the whole social distancing thing. I kept backing away as he enthusiastically looked over the MG. He apparently has a couple of Lotus’s he is intending to restore although when he mentioned making one of them into a four door, and commented on how thick the fibreglass was, I began to question his sanity. It was about 7mins and 30 seconds into the conversation before he mentioned ‘Wheeler Dealers’ which is where my interest tends to tail off. Anyway, I think he was probably a bit lonely and confused by the whole Coronavirus thing. It goes to show how it is impacting people in different ways. I wished him well and off he went with his shopping trolley.

Final job today was to scrub the interior trims that I have. I just used some kitchen cleaner to clean the vinyl so I will fit what I have got tomorrow. There are definately some bits missing, so I’ll have to decide how to replace these and draft up an order to one of the many suppliers. I am keen to attempt a repair to the headlining, so there is not much stopping me cracking on with this now.