7&8 Nov 20 Starting progress

One advantage, perhaps the only advantage of lockdown is that we are forced to stay at home and not go ‘gadding about’ as we are normally inclined to do. So it was that after a most pleasant stoll in nearby Cirencester Park, Gloucestershire, as part of our permitted exercise, I found myself with a sunny late autumn afternoon to dedicate to the MG.

I decided to sort out the choke spindle on the carburetters (carbs for short) which I had managed to fit the wrong way around. What I haven’t recorded here is that I had previously corrected the throttle spindle which I had also fitted the wrong way around. Such is the lot of first time amateur car restorers such as myself, progress is riddled with little mistakes, however, with each mistake, I try to learn something. So to the choke spindle, which is an assembly comprising a spindle which sits within a cup on each carb (the MG has two). The choke mechanism operates when the choke handle is pulled on the dash. This causes the cable to tighten which, being attached to a lug on the spindle causes it to rotate. This rotation causes the choke mechanisms on both carbs to be operated because the ends of the spindles have lugs which fit onto the cams which themselves are on the end of the choke mechanism. The choke mechanism moves the needle inside each carb to richen the mixture, but also opens the throttle because the cams connect with a screw on the throttle spindle.

The fun begins when you realise that the spindles are not held in place in any way other than sitting in the cups on the carbs so when fitting the carbs you have to align the spindle ends (4 in total, 2 for the throttles, 2 for the chokes) with the cups, and have them aligned to the lugs (again 4 in total) while you are trying to to wriggle the carbs onto the mounting studs (4 in total). I make that around 12 points of contact which you are having to manage and it was certainly easier when I was able to phone a friend. To reverse the wrongly installed spindles, I loosened the carbs, but wanted to avoid taking them off as then you have to do the full accordian player impression as the two carbs writhe in your hands. The carb mounting studs are worth a mention, being located cruelly in the most awkward position and in perilous proximity to the razor sharp edges of the heat shield. It would be good to have three elbows on your arm at this point rather than the inadequate one we have to deal with. I won’t bore you with a blow by blow account, but suffice to say I got it all done in two attempts and only one skinned knuckle. I then fitted the air filters and went for a start up.

I connected the battery (ignition switch solution still pending), heard the familiar ticking of the fuel pump and turned the key. One click and then nothing. Mmm. I tried my spare battery, and it cranked over willingly but wouldn’t fire. Then I remembered to reconnect the coil wire I had disconnected. This time the engine started straight away, with full choke of course, and settled at a fast idle. After it had run for a minute or two I pushed the choke in and tweaked the idle speed to get it to idle correctly. I recorded the sound of the engine in the YouTube clip below. To get the authentic bass – use headphones. For an MGB is does sound rather tasty. Its obviously not set up right just yet, but it’ll do for the moment.

So that was a reasonable afternoon’s accomplishment. Today (Sunday) was a more gloomy day both weather and progress wise. A dull autumn day dawned and after finishing off the chores and watching Church online (another COVID consequence) I pushed the MG onto the drive intending to fit the engine fan I had bought recently. To get access to the pulley I determined it would be neccesssary to loosen the radiator and pull it away from the area. This is relatively simple on the MGB, being six 0.5″ bolts (what else) to remove. Having pulled the radiator back I realised that the fan I had bought was the wrong one – annoying as I thought I had searched it correctly. More catalogue searching required and another item for my MGB parts shop which I will be opening at some stage to sell on all the surplus parts I have amassed over three years. So I had to pointlessly put the radiator back again. It was then I remember that fitting the radiator is more difficult than removing it. The radiator is mounted by the aforementioned six bolts to a steel shroud which is fixed with eight bolts to the inner wings. The challenge is to get this all to align. The shroud in my MGB, despite being resplendant in shiny black from the paint shop, is I believe a bit warped. The off side is particularly difficult and I had to loosen all the bolts on the radiator and shroud on that side to get each bolt to bite on its thread. Having had this difficulty before, I was up to the challenge this time, and a bit of thinking and remembering got the job done in the end. All helped along by my Radio 4 soundtrack in the background, latterly a re run of ‘Just a minute’ with the late Nicholas Parsons.

Thanks for reading – God Bless and Stay Safe.

17 Oct 20 Jaguar Mk2 Driving Experience

Something a bit different! Following up on my recent driving day experience in three modern supercars, today I travelled with Helen to Upton Warren in Worcestershire to drive a Jaguar Mk 2. This was a present for my 50th Birthday from our dear friends Sarah, Lewis, Martha, Freya and Joe and much appreciated – thanks guys. We had an unhurried drive up from our home in Wiltshire and the weather stayed clement, a good start. We arrived at ‘Great Driving Days’ which was situated on an agricultural yard next to a field of Highland cattle. We spotted ‘our’ car on the yard and eagle-eyed Helen spotted that one front corner was pushed in. The guy explained that the car had been ‘bent’ when out on loan earlier in the week, ending up in a ditch. Oh dear. We were offered a swop, but my heart was set on the Mk2. We had a quick overview of the controls and pressed the starter button. Amazingly, it fired instantly, which was impressive. Later my Dad would relate that a friend of his had a Mk2, back when he was a young man, and they always reckoned that his car started before your finger reached the button! I gingerly blipped the heavy throttle, selected first and eased out the clutch. With a whine from the gearbox, the old Jag pulled smoothly away. We rumbled along the track to the main road and with Helen in charge of navigation, turned left onto the main road.

First impressions: Pick up was lively, but I was having some trouble initially with negotiating the gear change from 2nd to 3 via quite a wide gate while smoothly feeding in the throttle. Compared to my daily diesel SUV, the throttle response was really crisp so blipping the throttle when changing down was a real pleasure. The other first impression was of the slow steering, which although it had been converted to power steering had a slow initial turn in with it needing a good quarter turn on even the slighest bend. I was having to recallibrate against modern cars – the slow steering, crisp throttle response, the long throw and wide gate of the gearbox. So I was concentrating quite hard at this point, but appreciating the sound effects of the straight six up front.

After a few minutes I was starting to get to grips with the controls and starting to just enjoy the experience – the view down that lovely bonnet with the leaping Jaguar. Feeling more confident, as the first straight bit of road appeared, I tentatively pushed the throttle all the way in third and allowed it to build revs. This was fantastic, over a certain RPM, the engine note changes and becomes a deep-throated roar accompanied by a decent shove in the back. I looked down at the speedo and we were only doing about 45mph! The beautiful large rev counter was unfortunately not working, so I changed gear ‘by ear’ and I was respectful of the age of the vehicle. All the gauges were reading well – temperature was steady (it had a later electric fan), oil pressure held up, although it dropped at idle and the voltmeter stayed put. The dash is all wood, with great big old gauges with retro script and a row of toggle switches, it really is iconic.

The route we were following had a really good mix of roads, from quiet country lanes to open B-roads and a little bit of A-roads. During the drive, I was starting to discover a dual character to this old Jag. Its first character is all about burbling around in the big squishy seats, enjoying the view and using the torque of the engine to pull you along with minimal changing gear. As we pottered through a narrow country late, I pulled over to let some cyclists come through – the lead cyclist mouthed ‘nice car’ and waved. I agreed! The other character of the car is when you have room to give it some welly in second, snick it up into third, give it some more welly, attain a pretty good turn of speed and then fling it into forth. For an old car, the acceleration is brilliant and the gearchange is really slick once you’ve got the feel of it. In this mode, the Jag is a racing machine, apparently lapping up this kind of treatment. It has to said, with open throttles, at higher revs, it was very noisy, with induction roar, exhaust blare, gear whine and wind noise all contributing to a glorious din. In addition, heat was wafting up the gearlever gaiter from the gearbox – a multi sensory experience!

With my amateur mechanic hat on, I would say that the Jag was idling at too high revs – I wondered if they had set it this way to help people to avoid stalling. Also, the particular car had a few defects which it would have been to rectify, like loose door capping and a stiff throttle pedal which could have done with being eased to make it drive smoother, but I’m being a bit picky.

We stopped for the obligitary photo shoot with Helen taking her usual high standard of still photos and video on her iPhone, including her jumping out of the car and energetically running up the road to film the Jag driving through a ford.

All too soon it was time to return the Jaguar to its home and we arrived back safely to the farm with Jag in one piece. A really enjoyable experience – now to the pictures!

Two hands on the wheel please Mr Trigg – look at that iconic dashboard
Nice artistic detail shot from Mrs Trigg
Mrs Trigg looks adoringly across as her husband manfully tames the big cat
Iconic photo of classic car driving through Ford

So thanks to the Boddy family, Helen and to ‘Great Driving Days’ a small business based in Upton Warren. I would highly recommend them based on this experience. For anyone else doing one of these, you need to set your expectations. These cars are in working order – don’t expect concours condition – and being classics, they are noisy, smelly and antiquainted. That’s the appeal and it was an unforgettable, and repeatable experience!

9 Aug 20 Fuelling around

So having demonstrated that the MG would start, it was time to connect up the fuel pipe and provide a reliable supply to the carbs to sustain running. I had a reliable assistant in the form of Matt (Ellie’s boyfriend). First we bought some fresh fuel and charged the tank with 5 litres. Next we connected the fuel pump wiring, connected the battery and heard a reassuring tick from the pump (err, surely after you turned on the ignition…). After a short while we were concerned that no fuel was flowing through and sure enough, on checking I found the pump was plumbed the wrong way around. I wonder who did that?

After a bit of replumbing and we were back in business although still there was no fuel feeding through to the filter let alone the carbs. Vaguely remembering something about air locks we released the pipe at the carbs end and with a hiss we started to see fuel travelling through the filter and turn up to the carbs. Progress!

But this wouldn’t be the Relentless Duck blog without some ‘issues’ and without detailing all the challenges, we did have a leak out of the fuel sender unit. Not being sure why this was leaking we set up a fuel can to catch the drips until the level was low enough for it to stop. The following day, on a break from work, a YouTube video showed how this should have been tightened up. Another day, another thing learned.

With fuel to the carbs, surely the MG would now fire up and continue running? Sadly not, the carbs refused to take the fuel and the removal of the lid from the float chamber revealed it to be dry. Oh dear. Further investigation needed, the outcome of which will be covered in a future post

1 Aug 20 a step forwards

I’ve had a problem with oil leaking from the oil filters area for a while and this has prevented me progressing the engine start because cranking the engine resulted in a pool of engine oil under the car. Having had several goes at refitting the oil filter to oil cooler union, today I used my brain and had Helen in the car cranking the engine over and me looking to see where the leak was coming from. Turns out the leak was from the oil filter ONTO the connection so I was looking in the wrong place. So my focus turned to sorting this connection out and following a phone call to Dad I removed and refitted it. No leak on cranking! Problem solved. I couldn’t resist cranking the engine over to fire (which it didn’t) but I did check and I was getting no spark so at least I know one of the problems to sort out.

This lovely engine bay will sound nice too one day
Oil everywhere but where from!

Back to earlier in the day and ongoing (and off going) saga of the doors and their glass. I had previously fitted the quarter lights but on inspection the runners were perished so I recently ordered some new one from Moss and had stripped them down. So while British Grand Prix Practice and Qualifying ran on I sat in the lounge working the new rubbers into place using a blunt ended tea spoon. Apart from where it dug into my palm painfully it wasn’t too bad and I followed the general approach that Andy from Wiltshire Windscreens showed me when he fitted the front and rear screens. So with these done I loosely fitted the back in. I will tighten them when I get the glass as I think you need them loose to get the whole mechanism in and then you tighten it all up.

Also in preparation for the glass (which I need to order) I removed the lower bracket from the rear glass stay. I have ordered new ones of these with nice new felt lining but they don’t come with the bracket. Rather than put the old brackets on as they were. I decided they would be better painted. I used a Hammerite black straight to rust paint, brush applied. It doesn’t need to look good but it should be protected against corrosion hence this approach. I was a bit delayed in fitting the stays as the paint is still drying so I will need to fit those when I next get the MG out.

Waiting for these to dry before fitting

So that’s about it. Keith the TV aerial guy was passing with his mate and said Hi. A couple of other people nodded their appreciation (or sympathy or contempt it’s hard to tell) so it was an encouraging day on the MG. Last thing to say is that to save my back I towed it out the garage this morning with my CRV which worked reasonably well although I did need a willing assistant which was of course the ever patient Helen.

A closing thought about gratitude…

30 Jul 20 Putting my back into it

I was motivated to get outside after work today and do something useful on the MG. I have for a long time bemoaned how I routed the rear loom which turned out to foul the internal trim panels due to a temporary cognitive failure on my part. So I decided to reverse this and find a better route. Reversing the install turned out to be much simpler than I thought.

I then had to work out a better route and curiously it is remarkably unclear what this should be. After a bit of trial and error I have found a route which allows the loom to reach all the right places and also looks like a reasonable location to be clipped in place out of the way and logically. At least I hope so.

It was good to make some progress after having had a lot of (admittedly not entirely unpleasant) distractions. The only down side was a twinge in my back as the MG is getting heavier the more parts I bolt on, and my back is getting no stronger. I may revert to towing it up the drive until she’s a runner.

28 Apr 20 Daft cat

Just a quick entry to record this picture of our daft cat. My daughter popped into the garage to access the freezer and as often happens, the cat dived in to poke around the garage in search of a mouse (although she is a useless hunter and there are no mice in the garage, unless you count the 2 x frozen mice we have kept for the in-laws pet snake for when lockdown is over). Anyway, standard procedure is to close the door and leave her in there for ten minutes. She’s usually ready to come out. But tonight she decided to stay in the MG and Lou managed to capture this shot – daft cat. Pity she can’t sort out the timing!

Stay safe folks – God Bless

5 April 2020 Door glass

A fine spring day (Sunday) as the COVID-19 lockdown continues. With the engine start programme on pause, I decided to continue refitting some of the extensive exterior trim on the MG. Having recently taught myself to pop-rivet, and finding out that is the most fun thing ever, I continued to fit the chrome drip rails and today managed to complete both sides. Just one clip missing which will either turn up or I’ll have to buy from Moss. I then turned to the door glass which I have been wanting to fit for a while. Unfortunately, the door glass is very badly scratched (I don’t know how) so I will need to replace them, however, I decided that there was merit in having a go at fitting them anyway as a sort of trial run for when I get the new / second hand ones. Tricky to justify buying new glass at the moment as I can’t collect from Moss (shop closed) and the cost of shipping glass is blooming expensive. Also, I would have to pry off the metal rails which looks tricky, so maybe I’ll source some second hand units via Ebay for as long as that remains. Anyway, back to today’s efforts which went alright actually. I had to remove the quarter lights and then reaquaint myself with the lifting mechanism which is a bit fiddly. I just looked at it and fiddled it around a bit until it fitted – it took a couple of attempts, I then dropped the windows in and they seemed to slide up and down quite convincingly After checking on YouTube I find that I haven’t hitched the glass properly, so something to sort out tomorrow on my day off.

Lots of people say hello as I’m working out the front on the drive, but one visitor today didn’t really understand the whole social distancing thing. I kept backing away as he enthusiastically looked over the MG. He apparently has a couple of Lotus’s he is intending to restore although when he mentioned making one of them into a four door, and commented on how thick the fibreglass was, I began to question his sanity. It was about 7mins and 30 seconds into the conversation before he mentioned ‘Wheeler Dealers’ which is where my interest tends to tail off. Anyway, I think he was probably a bit lonely and confused by the whole Coronavirus thing. It goes to show how it is impacting people in different ways. I wished him well and off he went with his shopping trolley.

Final job today was to scrub the interior trims that I have. I just used some kitchen cleaner to clean the vinyl so I will fit what I have got tomorrow. There are definately some bits missing, so I’ll have to decide how to replace these and draft up an order to one of the many suppliers. I am keen to attempt a repair to the headlining, so there is not much stopping me cracking on with this now.

14 Mar 2020 Electrical Issue

So today was looking good to get the MG started. I borrowed a fuel bottle from my friend John and made a list of what I had to do. First job was to connect up the oil gauge pipe. This was relatively easy although now I look back at it, I have routed it through the same hole as the temperature gauge pipe so that will need re-routing – doh! Second was to disconnect the fuel pump because I was going to use a fuel bottle to feed the carbs, not the fuel tank (not wanting to leave fuel in the car for a long period). I also placed a bolt in the inlet manifold in lieu of not being able to connect the vaccum advance hose. I haven’t been able to work out how this works to date, but I figured the MG could start without the pipe in place. So far so good. I then attempted to connect up the ignition switch which proved to be more difficult than I had imagined because the terminal were not clearly marked so I had to guess which was which. I connected the switch in what I assumed was the correct way and proceeded to connect the battery. This is where things began to unpick somewhat. Dad has given me a foolproof way of testing the loom before proceeding to connect the battery. This involved using a test lamp and the idea was that if the light came on, the loom was not correctly connected in some way and had a ‘dead short’. Anyway I performed the test and the light came on, but I proceeded to connect the battery. On connecting the positive terminal, the cable and terminal sparked violently and started to weld themselves together. Okay so something not right here. So I abandoned the MG for the day, posted a query on Facebook and made a mental note to call Dad later.

I moved on to the Suzuki Cappuccino, my other ‘toy’ on which I needed to replace a corroded metal cooling pipe. I had bought a new pipe from Suzuki recently, for the princely sum of £50 (!) and thought I would get on with the job today as it was dry and I had come to a dead halt on the MG. There were five hose connections to this pipe and each of course had to be undone. Due to the angles, this proved challenging. The clips were those springy ones that you have to either have fingers of steel (I have soft office hands) to open or manouvre a pair of pliers to release them. It was a tedious process to get them all undone and even then the hoses were a swine to get off. I used my trusty heat gun to soften up the rubber and this worked really well. I managed to catch a lot of the antifreeze which poured out into my waste oil container. I then fitted the hoses to the new pipe using new jubilee clips and secured it to the bracket with two nuts. I took the opportunity to wash the overflow bottle and hoses while I was there and then filled the radiator with fresh ready-mixed antifreeze. I then took the Cappuccino for a road test during which I definately didn’t taunt a sleeping Mini Cooper, nor did I exploit the perfect 50:50 balance to zap around a couple of local roundabouts. That definately didn’t happen. All was well and after the Cappuccino had cooled, I topped up the radiator a little. I’ll keep an eye on the levels for the next few drives, but it was good to get this job done.

29 Feb 20 Working the problem

Confession time. I was banging on last week about having to lengthen the distributor wire, and why couldn’t it just be the right length and so on. Well I took a closer look today and actually I don’t need to lengthen any cables, I just need to connect it all up properly. That was a relief. I only had a very short time on the MG today, but I did spend some of it in finishing off connecting the front and rear loom. The rear loom connects to the main loom on a branch under the o/s near the master cylinders. I had previously connected some of the wires, but was having difficulty in getting others connected. Dad had suggested that I purchase a pair of bullet connector pliers and I used these for the first time in anger and they worked pretty well actually, although I had to salvage a couple of connectors from the old loom where the new one was missing some. So just one yellow wire left unconnected….any clues? no me neither.

So there you have it. The list of things to do before engine start is now quite short. Fit the vacuum pipes and oil gauge pipe, fit the battery, rig up a fuel bottle and that’s about it, apart from checking everything. As always, I have a busy couple of weeks coming up including a weekend helping at the in-laws farm, but soon enough I will be spinning the engine over. Exciting stuff.

In other news, I bought a cooling pipe for my Suzuki Cappuccino (pictured below). The existing pipe is very corroded and I didn’t feel safe doing any distance in it in case it let go. Anyway, a phone call to Suzuki Islington of Trowbridge resulted in a £50 card transaction and a few days later the pipe was in for collection. The Suzuki dealer was also a MG franchise and it was interesting to see all the new SUV MGs in stock, not that I am looking for a new car. On the way back I bought new antifreeze from Halfords and I checked out refilling the system on the internet. Looks relatively straighforward. I’ll fit the new pipe to the Suzuki when the weather improves.

22 Feb 20 Re-fuse-ing to give up

Spent a couple of hours on the MG this afternoon. It was cold and windy so I confined myself to the garage. First job was to finish off fitting the new rubber oil cooler pipes. I am replacing the nasty braided ones which are very stiff with OE spec rubber which is a bit more pliant. This is an awkward fit and it requires a bit of coordination because the oil gauge pipe has to be fitted AFTER the pipe cooler pipe because otherwise the spanner crushes the oil gauge pipe. Have a guess how I know this? After fitting the pipes I had to fit the hateful grommets to the radiator shroud which is another awkward job. Anyway it’s done now.

It’s all a bit congested here

Next I decided to progress the wiring loom connections. Last week I had to unpick the loom due to poor routing so this week I put some of that back. I connected the alternator which is easy then had to take the coil off to get that connected properly. So far so good. I then checked the fuse box which I wasn’t convinced had been connected properly. Rather than rely on pictures on the internet I actually used the wiring diagram and managed to use up all the available wires so it must be right! (It is right really).

So onto the next thing and I identified a problem. The distributor, which is a new unit from Accuspark needs power which it gets from the coil. Unfortunately one of the cables is not long enough. It mentions this in the instructions which cheerfully say ‘you may have to lengthen the wire’. I might write back to them to say ‘you could just supply the right length wire.’ So I need to grab a pal who can joins a bit of wire for me

This is the probably definitely correctly connected fuse box

Final task today was to fit an earth wire to the inner wing. The original bolt had been painted over and the head rounded off when I tried to release it. Even my freeze spray couldn’t rescue the situation so I did the brutal thing and drilled it out. I managed to then get another bolt to fit and job done. Not a bad afternoon’s work.

18 Feb 20 A day with Dad

A welcome visit from Dad who battled through, or rather around, floods in Gloucester to help me out today. Overall we made some useful progress, although as is often the case we had to go back to go forward. Before Dad had arrived, I pushed the MG out onto the drive and ended up unconnecting the loom under the bonnet because I now realise the routing of one of the branches was wrong and unless I pulled it all out, I wasn’t going to be able to connect the heater amongst other things. So a step back, but better to find it now than later.

Dad arrived and I prioritised having a cup of tea and an ice bun inside the house. You can’t mechanic on an emtpy stomach. So onto the work and Dad had expressed concern that we had not flushed the water jacket through. The heater control valve was clogged with rust on disassembly and so there was reason to suspect some corrosive sludge was lurking in the engine block. First we fitted the heater control valve to the engine block – this was to be our inlet for the flush – awkward job this as the bolts are inaccessible. I had tried new bolts, but these were about 2mm too long, so we had to dig out some shorter old bolts from the box of MG bolts. We then blocked up the top hose with a lump of wood wrapped in tape. With a finger in the temperature sensor hole and one on the heater rail pipe, we connected the garden hose and switched on. We got a dose of dirtyish water out the bottom hose, but not the expected deluge of rusty water. Holding my hand over the bottom hose built up a little bit of pressure, but we concluded that we had done what we could, so we refitted the radiator and hoses. This simple job actually took ages, because the radiator is awkward to remove and the hoses were not exactly co-operating either. In any case, we were in good spirits and Dad was great company.

Next Dad’s keen eye focussed in on the distributor which I had ‘fitted’ but he spotted that the clamp was on the wrong way and hence it wasn’t seated correctly, with the cap in contact with the steering column, which was a bit of a clue. Needless to say, he sorted that out although we weren’t able to accurately set the timing which needs to be done with a timing light apparently. Anyway, its in as good a state as it can be prior to attempting a start up in the near future.

What a top Dad he is

We broke for a sandwich lunch during which we were googling MGB engine bay pictures and researching bullet connector pliers. With a target of filling the car with coolant, our afternoon was spent in fitting and modifying in some cases the hoses of the cooling system. Facing a challenge with routing of the capilliary tube for the temperature sensor, Dad came up with a clever idea of using the bottom bolt of the heater control valve to fit a cable clip, lined with rubber hose to gently locate the tube and stop if waving around in the engine bay. Execution of this brilliant idea came down to me, and it was a pig of a job (thanks Dad) as the 7/16th bolt is very awkward to reach and one of those situations where you get about 1/4 of a turn at best with each placement of the open jawed spanner. Couldn’t get a socket or ring spanner to it, so just had to plug away. I only nearly cried once, but that was the wind in my eye. We then wound the excess length of the tube into coils to deal with any vibration in use.

Time was ticking on and Dad needed to get away for 3:00pm as flooding on roads near his house was a real risk, not to mention that he had worked bloody hard all day and is 73 years young. Of course, we made it with minutes to spare – all hoses complete and coolant topped up, and the car pushed into the garage missing a downpour of heavy rain.

So thanks to my Dad – he knows his stuff, he gets stuck in, he’s always looking to improve everything he tackles, he doesn’t let things get him down, he’s great fun to be around, are you getting the picture? He’s one in a million, thanks Dad.

15 Feb 2020 Avoiding Storm Dennis

Seriously stormy weather today in Wiltshire, courtesy of Dennis, so the only option for progressing the MG was to work within the confines of the garage. This limited what I was able to do, but actually we made some good steps forward, so not too bad at all. First of all, a couple of photos attempting to record just how grim the weather was. Its difficult to capture it, but it was just relentless wind and rain.

Decided to fit the radiator and hoses today. I bought the radiator and new hoses over a year ago, and they’ve just been sitting there waiting installation while I have built everything else up. The installation, which should have been a simple bolt on, took a bit longer because the radiator bolts did not align with the radiator shroud to which its mounted. I had previously fitted the shroud so envisaged just bolting it on. I attempted to overcome the misalignment by pushing and pulling, but that didn’t work. So I decided to unmount the shroud, fit the radiator to this, and then fit that to the car (via captive nuts on a lip on the inner wings). This method worked well and as I removed the shroud I could see that the holes for this were slotted so maybe that’s how the misalignment occured. I had plenty of practice putting the bolts on and off, that’s for sure. Next task was to fit the hoses and although these were a bit fiddly, a bit of patience and some Fairy Liquid got them mounted and I then fixed them with jubilee clips. I have now reached the stage of needing to have jubilee clips all facing the same way and I had one hose fitted before I realised the clips was the wrong way around, so that had to come off again! As I was in the area, I fitted the thermostat housing gasket which I had missed off when I fitted it earlier. Nice new shiny nuts and washers improved the look too.

While fitting the bottom hose I briefly managed to get my arm stuck between the alternator and the radiator. I had my sleeve rolled up and was reaching right down to fit the hose and as I went to pull my arm out, nothing happened. My arm just stayed put. This has only happened once or twice on this project, but it it is weird when it happens because you sort of think ‘well it went in, so it has to come out’. From experience, the thing to do is to think your way out as opposed to tugging to get free which just hurts and doesn’t always work. Anyway with a bit of a wriggle, I was free with no need to undo the radiator I had just fitted to free myself.

After this drama, I fitted the radiator stays. I had bought replacements for these, and also repainted the originals. The originals fitted better when I offered them up, so I fitted those, the others will go into my surplus sale box. On the near side, I had to replace one of the wing bolts, as the radiator stay relies on this for its fixing, and the bolt fitted was too short. I fitted a longer bolt and that all worked, but now I have one steel looking bolt, and the rest painted white. Something to touch up at some point.

I decided to re-use the original radiator cap, but it was a bit scruffy, so I cleaned it up using first my Dremel tool, then sandpaper and then metal polish. Quite pleased with the result pictured below.

The last job I tackled was to fit the proper spark plugs which I had bought over two years ago when I started the engine to see if it would go. I have already gapped them before, so it was just about fitting them. I removed the old faithful plugs that came with the car which only served the purpose of plugging the hole when the engine was out the car. I checked the plug leads were fitted in the correct firing order and they were.

Away from the garage I braved two forays outside to Halfords. First time to buy a battery as recommended by someone on the Facebook MG restoration page. It looked a bit big, but I thought I would trust the advice. Second visit to Halfords was to take the battery back and this time taking along my existing battery as a size comparison. Halfords were very nice and I did a quick exchange to obtain the correct size. I like our local Halfords, they have always been helpful and although they don’t stock everything, they’ve been good to me and don’t have any thing bad to say about them. The new battery is to give us the best possible chance of a successful engine start soon.

Feeling quite satisfied with progress made today